bear24rw
07-10-2007, 20:42
Hi, im trying to force my 04 RC into automode by setting the team number zero. I dont have radios but i have it tethered. I power up the RC and i then change the team number to zero on the OI, i then untether and reset the robot controller.. all the LED's are green but its not in autonomous mode. I have figured out that it hangs on the putdata function at the end of process_data_from_master_uP()
Any idea on how to fix this?
<edit>
nvm i just realized that i thought it was hanging because i was not seeing my printf's but i forgot to include stdio in user_routines_fast
</edit>
Any idea on how to fix this?
<edit>
nvm i just realized that i thought it was hanging because i was not seeing my printf's but i forgot to include stdio in user_routines_fast
</edit>