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Re: Bridge device failure fix
We came up with this around week 2. Only mistake was direct driving it with a PG71. Worked fine on the practice bridge, but the real thing would've laughed at it. So we're running on a 256:1 P60. After shearing pins, replacing them with PG71 pins and then shearing sun gears, we put a latch on it. Otherwise it works good. An interesting point is that the angle has relatively little effect on the holding torque necessary, unless your pivot is well above 12".
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Re: Bridge device failure fix
Our team had that in our first regional, but we still weren't able to lower the bridge. I assume it's lack of torque in our drive train, but I want to get other opinions.
We're using 6-wheel drive, with KOP Traction wheels in the center and omni-wheels for the other four. Each side is driven by one CIM (which I think is our problem) into a CIMple box, and the chains are all 1:1 ratios. Another problem was that a last-minute shooter design change forced us to move the arm to the side, and we couldn't afford the weight of a second arm (connected so as to not violate the one appendage rule) on the other side. We plan to fix both of those problems for our next regional, and I hope that will allow us to easily lower the bridge. |
Re: Bridge device failure fix
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Re: Bridge device failure fix
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Re: Bridge device failure fix
beiju
Our team had a similar device mounted off to one side of a wide robot. It was not very effective. The drive train has 4 CIM motors each driving a Mechanum wheel. The robot would pivot toward the other side when the bridge pusher contacted the bridge. We concluded that only the two motors on the side with the bridge pusher were contributing thrust towards pushing the bridge down. We are in the process of replacing it with a sturdier device that is mounted in the center and powered by a geared-down van door motor. Our weight estimates show that we should be able to install a second pusher arm on the shaft of our mechanism. One of the reasons for gearing down the van door motor is to get greater torque. This may allow us to help balancing by holding the bridge up and lowering it slowly, damping the sometimes violent oscillations. The other reason is to slow down the motion of the mechanism so that the limit switches have time to work. The first one that our team built was directly powered by a window motor. It would come down with a loud "whack". It eventually destroyed the limit switch. The motor only had to rotate about 90 degrees to deploy the mechanism and at 84 rpm, that takes only a fraction of a second. It is quite possible that the damage to the old arm was self-inflicted when it smashed into the end stops. |
Re: Bridge device failure fix
I'd be interested to know how you get a 20 degree angle with sides of 14 and at least 8?
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