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why did technokats have lots of problems?
Anyone know why the technokats had so much trouble this year with their transmissions or whatever was preventing them from moving to well, so often?
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Heh quite an amusing story,
We were running great until one match the victor attached to our left side drill motor blew because metal shavings from the gearbox shot up into it and yeah, it stopped working. We replace it and go to our next match were the same darn thing happened on the right side to the drill motor BAH! Saturday we had no problems until we got to the finals and we had a major collision during auton mode and we never had full voltage for the rest of the match. Afterwards we pulled the bot off to the side and checked it out and from that collision the nut on the fuse pannel for the main breaker ground wire came loose and the crimp basically never was fully connected...doh! It wasnt my fault, but it was my responsibility so I am fully taking the blame for it. Oh well. |
here's another technocat-related albeit slightly off-topic question:
why did the technocats switch from a six-motor drive assembly (drills/chips/fisher-price) last year, to a four-motor drive assembly this year? What it basically boils down to is that my team is looking into a six-motor drive four next year, and I'm trying to do some homework as to wether or not it is feasible/useful, or simply overkill. |
Why you ask?
heh its because we pulled way too much current last year and frequently tripped our 60 amp breaker. Plus this year we used 9 motors and we needed the two FP's for our arms ;) Im not trying to discourage you from doing it...more power to you |
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so, from what I'm hearing, the general consensus is that its not a good idea?
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Jake, use your resources wisely....dont sacrifice a motor to your drivetrain if you could find other usage for them that would be better....the way we did it was overkill, but heck who knows what you guys could design |
another reason i could think of...
This years drill motors are alot more powerful than last and that will help make up for the power loss associated when dropping out the 2 FP motors. I think the 4 motors they used this year were probably just as powerful as the 6 motors they used last year. |
what i want to know is how much advantage do you get by adding motors beyond 2 per side (if you're doing tank drive)? It seems to me that no matter how carefully you calculate your gearing there'll still be some variance in the actual motors (especially after a few rounds of competition) so won't they either wind up fighting each other, or one motor wind up pulling all the others behind it?
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Ready for 3
The gearbox this year was actually ready for the addition of the Fisher Price motor as you can see in the picture. We decided against it because we needed the motors for the wings.
http://www.pictars.com/0412003/03-45-gearbox.JPG (copy & paste link) |
do you think that your three motor design would have continued to trip stuff even with the new 120a breaker?
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Before you do that i would work out the power you could achieve with just the CIM and the Drill's. Those 4 can pull 160 amps which theoretically is enough to trip the breaker(it really won't). Secondly you need to find really high traction wheels if you really want to use that power. i think the technokats tore up the carpet once with that 6 motor system at nats(they had those metal treads). It might have been a different team, but either way they had more power than they could use.
If you're working on it now. You have time to really calculate it all. Thats what i'm doing. But i'm going for something slightly different. My plan |
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basically right now with the motors and assemblies we have delt with, 6 has been overkill...keep working on it though, maybe FIRST will give out new motors next year (this isnt a confirmed fact nor a rumor.) |
i hope they don't put out new motors. I find it pretty annoying. We have to design new mounts and interfaces for them. Instead of improving old ones.
Just as a note though, that 60 amp breaker could do up to and sometimes over 200 amps for some period of time. It could consistantly do 120 amps easily(the matches are only 2 minutes). Thats why i was slightly worried that the new breaker would actually be tougher to use because it would be more accurate. Turns out its just good/bad. My team probably pulled about 160 consistantly this year and our breaker never tripped(our robot did... but thats different). |
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