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Robot doesn't turn in high gear
well i know that this has been posted before but i also know that other teams are having this problem and im sure they want all the info they can get. it seems that we are not getting the full potential out of our andy mark shifters not in low gear, low gear works great, but in high gear. we cannot turn in high gear, the battery voltage on the O/I drops and the motors seem to stall, we are using 1 big cim and 1 little cim on each gearbox any input????
would it be a smarter choice to switch to 2 small cims on each gearbox?? thanks |
Re: AM shifter problems
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Re: AM shifter problems
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Andy B. |
Re: AM shifter problems
Also it will help us help you if you give a complete description of your drivetrain/chassis....ratios, width, wheelbase, number of wheels, tread type, whether the center wheels are lower than the end wheels and by how much, etc.
Long, narrow, 4 wheel robots with sticky tread, and not much final drive reduction, just don't turn easily. Wide, short, 6 wheel bots with lowered center wheels, not so aggressive tread, and more final reduction turn just fine in high gear. |
Re: AM shifter problems
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(How to Be Sure Your Robot Will Turn)</edit> http://www.chiefdelphi.com/media/papers/1443 |
Re: AM shifter problems
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Re: Robot doesn't turn in high gear
its definatlly the fact that we have the 1 big and 1 small cim, were going to have to swap over to 2 small cims
thanks guys |
Re: Robot doesn't turn in high gear
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How many teeth are on the sprocket on the wheel? How big are the wheels? |
Re: Robot doesn't turn in high gear
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Re: Robot doesn't turn in high gear
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I'm also inclined to pin it on a configuration issue along the lines of sanddrag's post, we can't be sure without getting more details (sprocket sizes, wheel coefficients of friction, etc.) without pictures (CD-Media is a wonderful thing) or more details. |
Re: Robot doesn't turn in high gear
I've seen their setup first hand. They have four 8"(?) custom traction wheels in back and 2 AM omni's in front. After watching them at Philly, their low gear was relatively fast, very similar to our speed, but we used the AM Single Speed Gearboxes on a 1 to 1 output to wheel ratio. So I would suggest that you increase the size of your sprockets on the wheels, decrease the size from the gearbox, or even both. That hopefully should help with the turning problem.
-Chuck |
Re: Robot doesn't turn in high gear
Team 418 used a 6 wheel drive, 4 small CIM-DeWalt transmission drive train. We lowered the center wheels 3/32", which is enough to sink the center wheels in the carpet, but still have all 6 wheels contact the ground. In 2nd gear we realized we had some difficulty turning (the RC was resetting, I believe), and after talking with the electronic guys we think we figured out why. When designing the drive train, I figured we could run each small CIM at 40 amps (since they are on a 40 amp breaker); however, I was informed that the power distribution block is rated for 85 amps (I'm not exactly sure, but around this number). This means we weren't getting the current, and thus the torque, we had planned on. Perhaps you guys are facing a similar problem.
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Re: Robot doesn't turn in high gear
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Re: Robot doesn't turn in high gear
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Ex. 4 ft #6 wire, breaker panel, one victor, 4ft of #12 from fuse panel to Victor to motor, 20 connections= (4x0.5)+1+4+8+20=35x0.1=3.5 volts drop in all losses at stall. This translates to a loss of about 1/3 of the available current or about a loss of almost 100 oz.in. of torque and a drastic change in the efficiency. |
Re: Robot doesn't turn in high gear
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As for the resistance in the circuitry, we kept the wire lengths to a minimum, and will definitely be more conscious of it in the future; however, I do not understand how this would fully explain our problem. At 40 amps, a small CIM outputs ~.8 N*m (please correct me if my calculations are wrong), and IF we could run them significantly beyond this, say, near stall current, then even if you take the ~2.2 N*m stall current then the wire resistance would have to be somewhere around 76 WF. Though I am not the most familiar with our electronics system, I am confident it does not have this much resistance. Now, I did make several assumptions when calculating the torque needed to turn in 2nd gear, so in actuality .8 N*m of torque might not have been enough; but, assuming that the difference is negligible, how do you explain the problems we faced? Also, I have just talked to our electronics/code mentor and he suggested that we bypass the Rockwell block to see if it is (at least in part) the problem. He also suggested we monitor the voltage on both sides of the Rockwell block using a USB DAQ, so when we get those results I will make sure to follow up on this. |
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