Quote:
|
In addition to that, our robot at one point lost the link to FMS just as the match started, and then magically gained it back immediately when the match ended. During this time, we found out their last reading for our battery was 3 volts, and when we checked, it was actually still charged to 10 volts, so an underpowered bridge is most likely not the issue.
|
10 volts (which is really, really low btw) at idle could certainly drop to 3 volts when you start actually driving.
Here's an alternate theory:
-The 10V robot started the match, and as soon as the drivers engaged the power-hungry main motors, the voltage dropped so low the various voltage regulators couldn't keep the cRio and bridge functional
-The 2011 bridge takes about 90 seconds to reboot in our timing
-By the time the bridge rebooted and reconnected to FMS, the match was over.