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Re: Programming goofs!
In 2008 at Lone Star, our robot was supposed to make 3/4 of a lap, but instead our power kept shorted out and it restarted the program an we slammed the wall at full speed went up on three wheels (of 6) and turned around, went full speed back and nailed our team mate who didn't have a autonomous mode. Our robot was unharmed and hitting the wall the second time it fixed the short. We one the Motorola Quality award and the judges told us that was why, because other robots would of broke down after that kind of hit.
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