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Re: RobotPy 2011.3
now that you've confirmed those steps, i'm running on a new theory.
i think flashing to c++ might not have worked correctly.
we've had it fail to switch before. i'm kicking myself for not thinking of it at the time.
now we're going to retry flashing until a the sample c++ program runs. then we'll load the python interpreter.
i'll let you know how that works this weekend.
i've talked to a couple people on other teams who also have had trouble flashing. is there something better than just retrying until it actually flashes? one guy suggested something about dip switches on the bot?
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