Quote:
Originally Posted by sergioCorral842
So I believe I might have figured out the issue. Since we are using 6 cims on our robot, when we go full speed, the amperage caused by the cims could be causing the radio to go bad. I am going to write some code that prevents the motors from instantly going to full power. Instead, it will accelerate to it. Will post back if it works.
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If you have the radio wired properly, it should not be caused by current draw. However, if you have your radio placed near your CIM motors, you could see an issue.