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Code suddenly not working
We are a second year team and pretty familiar with labview. We made a new robot project and added our our drive code. It worked. Then we added 3 other Sub Vi's in the tele-op Vi. These VI's execute an encoder, a gyro (drive straight), and a shooting sequence. We deployed the updated code and the drive system stopped working. Between the two deployments we changed the motor controllers (we have changed them in the programming as well). The Robot code Boolean on the driver station keeps cutting out and then the CRio discontinues communication, however the robot is still on and connected. We have run a default program and it works. Any ideas???/ please help!!!
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