Quote:
Originally Posted by NotInControl
With the motor removed, do you still have a short to the frame?
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I don't remember :/ I'll check it first thing tomorrow
Quote:
Originally Posted by NotInControl
How is the dlink wired? Is it going to the proper port on the power distro board and through the 12V-5V regulator?
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Yes
Quote:
Originally Posted by NotInControl
Is the communication intermittant only when the robot is running its motors, or if it is just on, you notice comm dropouts.
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Only when enabled (even if no motors are actually running). - Which may hint that there is another short somewhere?
Quote:
Originally Posted by NotInControl
Posting your DS logs might help.
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Tomorrow i'll be in the workshop and post those.
Thanks for helping