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Unread 15-03-2003, 19:26
Alex1072 Alex1072 is offline
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#1072 (Harker Robotics Team)
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Join Date: Jan 2003
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We were having issues with our robot going berserk too, but we wern't using multi slot programs. Make sure you never output 255 to a PWM. It makes the robot go crazy, and some very odd (and hard to trace) things start happening. IE. We outputed 0 to both relay banks. If the PWM output was set to 255, the relays would randomly turn on anyways.