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Unread 15-01-2016, 16:22
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Alumni of Team 2053 Tigertronics
AKA: Drew Williams
FRC #2053 (TigerTronics)
Team Role: Programmer
 
Join Date: Jan 2014
Rookie Year: 2013
Location: Vestal, NY
Posts: 193
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Re: Strange issue with pushing code and running it on 2016 firmware

Quote:
Originally Posted by ozrien View Post
Can you try the following...
[1] Make sure a gamepad is connected and wired to slot 5 (the last spot) in the driver station. Change your source to use that slot, or just use an extra joystick/gamepad to ensure that slot is not empty. Either is fine.
[2] Then restart your project using the restart-robot-code, or redeploying.

Does that remove the crash symptom?
Why does that work! Thank you so much! This issue has been frustrating me for hours and a simple fix like this makes me a bit more frustrated because it is so obscure, but thanks! Is this a bug in the driver station code?
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