Quote:
Originally Posted by Joe Johnson
I know this is a long shot,
...
Something to consider. Hope it isn't a rabbit hole for you to fall down.
Dr. Joe J.
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The motor and gearbox is face mounted to 1/4in polycarb; the motor is 6 inches away from the chassis.
But interesting - we did ohm out each motor lead to the motor case. And that motor seems to have values that go down to .9ohm as we spin it by hand slowly.
What should that usually be?
We were going down a path of a loose USB tether, our RoboRio. But we thought that should always manifest itself with a "communication" error, and it was just simply disabling without any noted error.