Quote:
Originally Posted by s5511
During yesterday at tournament, our navX gyro sensor stopped returning values, causing our drivetrain PID to malfunction. The navX is protected by a plastic casing and is still directly plugged into the roborio. Are there any reasons that could cause the navX to stop functioning like this? We have been using it for over 4 weeks, and it has been working fine.
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Have you connected it to the rio via a USB cable? This will help to prevent RIO Stage 2 brownout from affecting the chip.
http://www.pdocs.kauailabs.com/navx-...oubleshooting/