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Re: NavX causing robot code to reboot
In 2015 we used the nav6 (predecessor of the navX). It used a serial connection to the roboRIO. We had issues with the roboRIO not working (not connecting or something like that). It seemed like we had to re-install the roboRIO firmware and re-image. Removing the nav6 from the robot fixed the issue. Anyway, we found that unchecking the "Console Out" checkbox in the roboRIO imaging tool allowed us to use the nav6 normally.
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