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Re: Motors and the High Port Numbers
Our lead programmer wrote his own PID code. In testing, nothing worked right using the high PWM ports. He used Generate_Pwms, too. When we moved the control to PWM 3 & 4, it started working. No worries, it only cost us a day...
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Exothermic Robotics Club, Venturing Crew 2036
VRC 10A, 10B, 10D, 10Q, 10V, 10X, 10Z, and 575
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