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Originally Posted by Booger
i loaded the defualt code from last year, and the robot just started going. It ran into a table and knocked everything over. Luckly it wasnt facing the otherway becasue it would have went down the road.
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Related bug, we had a 1 in an assembly level if check instead of a 0 (one of our less experienced coders put it there) and all the motors ran by the method just started running at full speed. Luckily this was early on and the motors were not attached to the bot yet.