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Re: Mistakes
1. During the build season, the programming team uploaded new code, and when we turned our bot on, the motors were Default all forward. Ran over a mentor. Luckily noone was hurt. We learned that the wheels should be raised when testing a new change ^.^
2.We spent about 3-4 hours, for 3 straight days trying to figure out why our robot wouldn't move. Turns out we were using 2 reciever boxes instead of 1 transmit 1 recieve >.<
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