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Unread 19-02-2010, 19:15
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Mark McLeod Mark McLeod is offline
Just Itinerant
AKA: Hey dad...Father...MARK
FRC #0358 (Robotic Eagles)
Team Role: Engineer
 
Join Date: Mar 2003
Rookie Year: 2002
Location: Hauppauge, Long Island, NY
Posts: 8,810
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Re: Count us in too...

Quote:
Originally Posted by pSYeNCe View Post
Team 2010 is also experiencing similar problems. We're getting a 1/2 to 1 second delay from moving the controls to a response. We don't have any loops other than the teleop.vi While loop that encompasses everything, so I think I'll try to time delay that a little bit and see what happens.
There shouldn't be a teleop While loop unless it is less than 1/50 sec.

Quote:
Originally Posted by jawebste View Post
Hello from 2145
Several of the Hook Motor Set Speed's are without a speed or motor reference. Of the three case statements for the Hook motor look at the False case on top, the False case in the middle, and the True case at the bottom. The pink wire needs to be wired across and the bottom speed needs a constant value.
I don't see anything else that would account for the delay you're seeing.
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