Quote:
Originally Posted by pSYeNCe
Team 2010 is also experiencing similar problems. We're getting a 1/2 to 1 second delay from moving the controls to a response. We don't have any loops other than the teleop.vi While loop that encompasses everything, so I think I'll try to time delay that a little bit and see what happens.
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There shouldn't be a teleop While loop unless it is less than 1/50 sec.
Quote:
Originally Posted by jawebste
Hello from 2145
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Several of the Hook Motor Set Speed's are without a speed or motor reference. Of the three case statements for the Hook motor look at the False case on top, the False case in the middle, and the True case at the bottom. The pink wire needs to be wired across and the bottom speed needs a constant value.
I don't see anything else that would account for the delay you're seeing.