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#16
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Re: Partial Jag failure?
Marshall - does it respond to PWM normally? Are there any signs of physical damage?
Al - Thank you for the very clear and informative post. The difference in total on-resistance between the Jaguar and the Victor is inconsequentially small. I think the Jag wins the numbers game, but not by enough to make an actual difference. The reason that the Jaguar uses fewer FETs is that it uses slightly more modern FETs that can handle more current per device. |
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#17
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Re: Partial Jag failure?
Getting back to the question of how the Jaguar failed:
Al's explanation of the desoldered current shunt resistor would make sense, except that the Jaguar says it's outputting 0v. I re-checked the diagram: the Jaguar measures its supply voltage, but not its output voltage. The output voltage is calculated from duty cycle. (Indeed, in the first revisions of the firmware, the output voltage was only GIVEN in duty cycle, on a range of -1 to 1.) Apparently nobody has had this exact issue before. I will check that the resistor is still connected, but I will also try reflashing the Jaguar, in case the firmware got corrupted. More info on the over-current: the Jaguar goes into over-current fault at 60A after 2 seconds. I was running an RS-775. (There were some binding issues with the jack screw on our arm) |
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#18
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Re: Partial Jag failure?
Well, it worked fine today. I even held it in a 41 Amp stall for 5 seconds.
There's only two causes I can think of. One is that perhaps it had tripped the breaker and needed "voltage enable" to be sent again. However, I'm pretty sure I would have seen movement out of it before that happened. The other is that today I'm outside at 15 degrees Celcius. Friday I was inside at 30 degrees. The Jaguar only said its internal temperature was 37 degrees on Friday. I thought it would operate up to 50. (Note: I haven't opened it up yet.) |
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#19
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Re: Partial Jag failure?
Marshall,
This kind of action leads me to believe there is a foreign body floating around inside. A look inside is warranted. |
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#20
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Re: Partial Jag failure?
I just checked inside.
No debris. No signs of heat. The resistance from 0v to vLow measures 0.3 ohms on my multimeter (the same as when I touch the leads together). I measured this between the 0v 6-32 screw and the lead of a low-side MOSFET. |
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#21
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Re: Partial Jag failure?
Quote:
Also...if the resistor got very hot...it would heat the PCB and itself. That combined mass might take a while to cool off even with the fan. Could it be that you melted the paste on that component and when it finally cooled off it closed again? One could also ask this question about the points to which the body of the resistor meet the areas designed to be soldered down. In other applications I've seen surface mount resistors recover from overload before but usually it alters the resistance which you might not be able to measure with that meter. If it has altered that resistance by some appreciable amount it'll alter your current measurements. Do these current measurements seem proper for the mechanism in question? Would there be some value in using a fixed, high power resistor as a load on the Jaguar and taking comparison measurements with another Jaguar? How about just trying to measure the current with another meter with a fixed resistive load? Last edited by techhelpbb : 20-03-2011 at 23:45. |
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#22
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Re: Partial Jag failure?
Marshall,
I am still going with my foreign body analysis. It is certainly possible for it to have been blown out by the fan. |
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#23
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Re: Partial Jag failure?
That works as a partial explanation.
Any idea why it would refuse to output power? (That is, it reported its calculated output voltage as zero) I'm guessing it's one of the fault conditions. I know of four:
Does the BDC-COMM display a Temperature fault or a Gate Driver fault in red, as it does the Current fault? |
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#24
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Re: Partial Jag failure?
Marshall,
I don't remember you mentioning a fault condition. It is possible that a particular fault will shutdown the voltage mode and the software may be written to report 0 volts under that condition. It is possible for the any of the sense circuits to have had a fragment causing a short to supply. Say for instance, a short at the input of the current monitor could have artificially raised the voltage input to beyond current rating. In the Tan Jag there is no feedback from the output terminals so the zero volt condition must be derived mathematically from internals. |
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#25
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Re: Partial Jag failure?
Ah, I understand now.
I was thinking of aluminum shavings only affecting large circuits, and destroying them in doing so. I hadn't considered that it might make a contact across a small circuit, and not damage anything in the process. Even more so, I hadn't considered that they might, in effect, put the Jaguar in a fault condition that it can't detect. I don't know that it was in a fault condition, but it's either that or the limits, and I'm pretty sure the limits were not active. These Jaguars really need a conformal coating. It would be interesting to compare the failure rate. In fact, if I had a few thousand dollars to spare, I would buy Jaguars, paint them with polyurithane, and sprinkle aluminum dust on them to see how well they survive. But because of the cost, I think that's something best done by TI. Last edited by kamocat : 21-03-2011 at 12:56. |
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#26
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Re: Partial Jag failure?
In response to your question in a previous post above:
"Does the BDC-COMM display a Temperature fault or a Gate Driver fault in red, as it does the Current fault?" In BDC-COMM itself...we find this in: bdc-comm.cxx Quote:
This is where they draw and hide the control for the fault indicator in FLTK in the file: gui.fl Quote:
So it does not appear that BDC-COMM considers the type of fault in setting this control's color. Have you seen it do otherwise? Last edited by techhelpbb : 21-03-2011 at 14:01. |
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#27
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Re: Partial Jag failure?
Quote:
They have a file in that firmware: adc_ctrl.c In that file: Quote:
Quote:
However, it appears in the older schematic they hid this divider in the schematic section for the power regulation. Look right next to C15 on the schematic...for the VSENSE tag. It's on the second page of schematics in the user manual and it's between the great big tag for "+12V POWER IN" and the 5V power regulation. In pins.h they define: Quote:
Last edited by Al Skierkiewicz : 21-03-2011 at 15:05. |
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#28
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Re: Partial Jag failure?
tech,
The VBuss is measuring input voltage so that the Jag can disable output when the input power goes down to dropout on the voltage regulators. The thought being that a significant load may be causing a large voltage drop in the input wiring. By disabling the output, the voltage can climb back up to full terminal voltage. There is no feedback in the controller from the output terminals. I changed the color on your post so people could read it. |
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#29
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Re: Partial Jag failure?
Quote:
They must use it for more than that...from readme.txt in the development kit... Quote:
Quote:
Last edited by techhelpbb : 21-03-2011 at 17:17. |
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#30
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Re: Partial Jag failure?
I presume in voltage control mode...this section of: controller.c is most critical.
Quote:
The do this by setting the target voltages to 0. What was this Jaguar configured for...brake or coast? Last edited by techhelpbb : 21-03-2011 at 17:16. |
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