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#13
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Re: 2012 Field Comm. Issue Logs
At our third Elims match at WPI, our bot executed autonomous fine. However, upon entering Teleop, spun in a tight circle, accepting no input from drivers and did not respond to an E-Stop command. What gets me is we were running fine throughout every other match that day. No new code that wasn't tested was loaded onto the robot, and *nothing* changed between our second Elim match to our third. (This includes electrical).
I'll post more details and the wacky logs later. EDIT: We used the 4-slot cRIO, LabVIEW, and did not use CAN. Dashboard: Edited version of the FRC Dashboard, did not cause any problems in the past. Radio: Not mounted near motors. 2012 KOP radio. Computer: MacBook Pro, 8gb ram, Intel core i3 running Parallels. (Had no problems with the FMS throughout the weekend once we set up the network settings correctly.) Vision processing: No. Ave. cRIO CPU usage: 40-60% Last edited by DominickC : 23-03-2012 at 06:27. |
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