Go to Post Just because a robot looks good and just because it is very well made does not mean that students were not involved in creating it. - Ryan Dognaux [more]
Home
Go Back   Chief Delphi > Old Forum Archives > 2000
CD-Media   CD-Spy  
portal register members calendar search Today's Posts Mark Forums Read FAQ rules

 
 
 
Thread Tools Rate Thread Display Modes
Prev Previous Post   Next Post Next
  #14   Spotlight this post!  
Unread 23-06-2002, 22:39
archiver archiver is offline
Forum Archival System
#0047 (ChiefDelphi)
 
Join Date: May 2001
Location: Pontiac, MI
Posts: 21,214
archiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond reputearchiver has a reputation beyond repute
Suck and See

Posted by Dodd Stacy.

Engineer on team #95, Lebanon Robotics Team, from Lebanon High School and CRREL/CREARE.

Posted on 4/2/2000 4:13 PM MST


In Reply to: We Need Help!!!!!!! posted by Travis Covington on 4/2/2000 10:55 AM MST:



Have you tried to localize where the problem lies? Being a hopeless dummy about all things electrical, here's what I'd try:

1) With the gearboxes in your normal driving alignment, block up the chassis and turn over the wheels by hand (backdriving the motors), left side, right side, forward, backward. If they don't feel substantially different, you are probably free of driveline problems.

2) Swap the PWM inputs to the two speed controllers, left for right, and operate the bot under the conditions that cause you problems. It will steer backwards, but you can adjust to that. If the problem swaps sides, its cause is probably in the control code or in the communication link. Using the tether could assess the latter.

3) Swap the PWM inputs back where they belong, and then swap the speed controller outputs, left for right. Try again (still steering backwards). If the problem swaps sides, its cause lies between the battery +12V terminal strip and the speed controller (including connecting wiring).

4) If the problem DOESN'T swap sides in 3), then I'd suspect a wiring fault between the speed controller output and the motor on the bad side, maybe an intermittant short to ground through some chafed insulation, maybe aggravated during match interactions? You can check this by disconnecting the suspect wiring and temporarily jumpering from speed control output to motor on the bad side.

I apologize for suggesting the obvious, but I always screw up when I don't ask and answer the dumb question before looking for detailed explanations.

Good luck,
Dodd


__________________
This message was archived from an earlier forum system. Some information may have been left out. Start new discussion in the current forums, and refer back to these threads when necessary.
 


Thread Tools
Display Modes Rate This Thread
Rate This Thread:

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

vB code is On
Smilies are On
[IMG] code is Off
HTML code is Off
Forum Jump


All times are GMT -5. The time now is 00:32.

The Chief Delphi Forums are sponsored by Innovation First International, Inc.


Powered by vBulletin® Version 3.6.4
Copyright ©2000 - 2017, Jelsoft Enterprises Ltd.
Copyright © Chief Delphi