|
|
|
![]() |
|
|||||||
|
||||||||
![]() |
| Thread Tools |
Rating:
|
Display Modes |
|
#1
|
|||||
|
|||||
|
paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Thread created automatically to discuss a document in CD-Media.
GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly by artdutra04 |
|
#2
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Awesome stuff Art, thanks for publishing this! Would you mind if this is posted on http://team1323.com/cad/pages/teamhosting.html ?
|
|
#3
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Very nice! A few questions:
- What was the thought behind the pneumatics on the intake assembly (i.e. why wasn't the intake static) - Did the empty cell mechanism end up working well? It looks brilliant. - And a non-design question: Why is the assembly made mostly of individual parts rather than sub-assemblies? Is there some advantage to doing it this way? Thanks for sharing this! |
|
#4
|
|||||
|
|||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Akash, you can post it there.
Quote:
The empty cell exchanger would work if you can get it close enough, and calculations based on robot bumper dimensions. Unfortunately, close enough was about two inches away in real world tests on the field. If there wasn't the rule prohibting expansions outside of the bumper perimeter, we could have made the fingers about two inches longer and it would have worked great. The only reason why there aren't too many sub assemblies is because I used folders to organize parts in Solidworks and used patterns whereever possible. There will most likely be more sub assemblies in our 2010 robot, as 2009 was the first year we modeled our entire robot and was a learning experience for us. |
|
#5
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
Once again, very nice!. I can't wait to see your 2010 CAD! |
|
#6
|
||||
|
||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
Of course, this assumes I haven't missed something... |
|
#7
|
|||||
|
|||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
|
|
#8
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
![]() Edit: Quote:
Really?!? Way cool! I didn't know that! |
|
#9
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
|
|
#10
|
||||
|
||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
This is my question to everyone, because this is automatically what I thought when I saw this robot last year. How many other people automatically when they saw GUS say to themselves "dang they got it dead on, and why didn't we think of that". It's an amazing design and above all it's simplistic, which we should all strive for in our designs.
And my question to GUS is this, how did you assemble your conveyer belts? 2228 used a very similar looking system. We took aluminum tubes and riveted wedge top in small sections to create channels for polycord to ride in. This worked pretty well, but on our elevator conveyer the polycord would often slip out, even in competition, and this proved the biggest disadvantage of our system. |
|
#11
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
|
|
#12
|
|||||
|
|||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
Originally the robot was designed to use foam between the polycord loops. This didn't work so well, as the foam from McMaster was a lot softer than we were expecting. So we replaced it with neoprene roughtop belting, with PVC pipe spacers on some of the rollers. The rollers were originally PET-G, but upgraded to aluminum as part of the 40lb allowance. We had some minor issues with the polycord loops "jumping" from one track to another, but these only happened if for some reason there was a Orbit ball jam in the system, and were usually limited to one or two loops total moving over one or two spots throughout the entire match. Because the loops were close enough together, this usually didn't negatively impact operation. Had we installed sensors on the robot to detect jams, we could have easily averted most of these issues. Other than popping one or two of the loops back into their tracks at the end of every match, nothing else on this robot ever required any sort of maintenance or repair. Our students even got into the habit of cleaning the fingerprints off the Lexan side panels in the pits just to have something to do. ![]() There was just a single part throughout the entire season (Connecticut, Championship, BattleCry@WPI, Where's Wolcott, Bash@theBeach) that required any kind of repair, and that was the 3/8" drive shaft on the ball intake bent slightly during a particularly nasty impact in autonomous at BattleCry@WPI. Even though it was bent and made angry noises, it still worked for the rest of the competition. We machined a replacement shortly thereafter, and it's been working great since. Here's some photos of the spacers from our team's website: ![]() (Hurray for the duct tape rule! We used small strips of it to prevent the #8-32 button head screws from backing out of the aluminum drive plugs, since even with Loctite we noticed them slowly backing out on the practice robot before our first Regional) ![]() ![]() |
|
#13
|
||||
|
||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
, and watch everyone in the room kick themselves, because if we simply had PVC rings like those we could have rapped and riveted the wedgetop just like we did, but that extra 1/4 or so that the PVC has in it's wall thickness would have created deep enough channels to prevent the polycord from jumping if not 100% of the time 99.9% of the time. And as the driver who piloted the robots elevator conveyerbelt and shooter I have to say this would have saved me the trouble of finding the perfect sequence of running the motor forward and backward to jump back to the right loop, so we could still shoot (surprisingly that actually worked on occasion but it's not something I want to see have to happen). Once again thank you to you and the rest of 228 for showing us your robot, and like I said before you guys have the right motto because simplicity is the key to any successful design.Also thank you to Jamie Kalb I think our mentors would be very interested in this approach to the design. |
|
#14
|
|||
|
|||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
Quote:
Hope that ends up helping! |
|
#15
|
|||||
|
|||||
|
Re: paper: GUS Team 228 - 2009 FRC Robot "Gus 11" CAD Assembly
WildStang has used lexan tubing for rollers like this. When they suggested we replace our cracked wooden one with lexan, we were amazed at the weight savings. We were also happy with the way the new roller basically shrugged off impacts without damage.
|
![]() |
| Thread Tools | |
| Display Modes | Rate This Thread |
|
|
Similar Threads
|
||||
| Thread | Thread Starter | Forum | Replies | Last Post |
| pic: GUS Team 228's 2009 Robot Render | artdutra04 | Robot Showcase | 16 | 14-02-2009 21:32 |
| pic: GUS Team 228's 2009 Teaser #1 | artdutra04 | Extra Discussion | 9 | 03-02-2009 13:31 |
| Post-Kickoff Pasta Dinner (Hosted by GUS Team 228 in CT) | artdutra04 | Fundraising | 0 | 19-12-2007 22:50 |
| pic: GUS Team 228 about to score golden tube | artdutra04 | Extra Discussion | 7 | 23-05-2007 19:54 |
| Introducing: GUS Team 228's 2007 Website! | artdutra04 | Website Design/Showcase | 18 | 20-03-2007 19:46 |