We afre seeing the same issue here. Spent a few days trying to figure out what was wrong with the rio before finding this.
We flashed with net console and CAN enabled for the black jags (didn’t try with can disabled).
Flashed to v27 innumerable times (flashing always worked fine), labview would not deploy code. I was able to ping and ftp into the rio without issue. The driver station would see robot comms on bootup momentarily, then it would lose it. I was able to successfully deploy from labview maybe 10% of the time. After a sucessful deploy, control through the driver station worked reliably.
This is pretty easy to replicate on our end.
The only fix that seemed to work reliably was to flah back to v25.
We seem to be hitting bugs this year every step of the way. Last week it was problems with the encoders. I don’t mean to complain, but these types of issues don’t help when your trying to teach the kids how something “should work”
What gives?
